Same here!...until I had an issue I was pulling hair over. The control pressure was high (almost matching PP) and I found a clogged WUR screen. Correcting that helped, but the pressures still acted odd. Trying to figure out WTH, I ran across the last docs. Long story short, the passage between the FD's WUR return line port and the piston's bore had a short section of the smaller o-ring plugging it as well...
[As a side note: None of those drawings reveal that you can adjust the PP via the carrier crush washer thickness, somewhat... ;-]